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DOW-UAP-D48, Department of the Air Force Report, 1996
Page 176
176 / 181
D.5.2 Thor and Thor-Boosted Failure Narratives
The following narratives provide information about flight failure of Thor weapons system
and Thor-boosted space vehicle launches beginning with the first Thor launch in January
1957. The narratives are numbered to match the flight-sequence numbers in Section D.5.1.
1.
101, 25 Jan 57, Response Mode 1, Flight Phase 1: Failure of fuel-system valve
resulted in loss of thrust. Missile fell back on pad after reaching an altitude of
only 9 inches.
2.
102, 19 Apr 57, Response Mode 4, Flight Phase 1:
Missile was apparently
performing normally until destroyed by the RSO at 34.7 seconds. Erroneous
DOV AP beat-beat plot showed missile heading uprange.
3.
103, 21 May 57, Response Mode 1, Flight Phase 1: Missile was destroyed on the
pad at T - 5 minutes. A faulty fuel-tank regulator and relief valve resulted in
ov~r-pressurizing and bursting of fuel tank.
4.
104, 30 Aug 57, Response Mode 4T, Flight Phase 1: Spurious signals in the main-
engine yaw fe~dback circuit resulted in missile breakup shortly after 92 seconds.
5.
105, 20 Sep 57, Response Mode 4, Flight Phase 1: Premature propellant depletion
• resulted in impact some 400 miles short of target.
6.
107, 3 Oct 57, Response Mode 1, Flight Phase 1: Main fuel valve closed 1.25
seconds after liftoff. Missile fell back on pad after reaching an altitude of about 17
feet.
7.
. 108, 11 Oct 57, Response Mode 4, Flight Phase 1: Due to a mechanical failure, an
abnormal main-engine shutdown (one second early) resulted in loss of the vernier
solo phase ..
9.
112, 7 Dec 57, Response Mode 5, Flight Phase 1: An electrical-system failure at 107
seconds produced an abnormal loading on the missile converter .. The missile
began deviating at 110 seconds and finally broke up at about 224 seconds (well
after MECO at 156 seconds). Missile impacted 200 miles downrange and 40 miles
left of flight line.
10.
113, 19 Dec 57, Response Mode 4, Flight Phase 1.5: Flight was regarded as
successful although there was no vernier solo operation and impact was 6 miles
from target.
11.
114, 28 Jan 58, Response Mode 5, Flight Phase 1: Guidance system failure at 95
seconds resulted in erroneous steering commands causing the vehicle to yaw left
and pitch down. Divergence began about 110 seconds and continued until the
9/10/96
167
RT!
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