Reader Ad Slot
Reader Ad Slot placeholder
If you would like to support SpookStack without paying out of pocket, please consider allowing advertising cookies. It helps cover hosting costs and keeps the archive free to browse. You can change this choice at any time.
DOW-UAP-D48, Department of the Air Force Report, 1996
Page 140
140 / 181
caused yaw and roll rates that the flight control system could not correct. As a
result, attitude control was lost and the thrusting sustainer pivoted the missile to a
retrofire attitude before the vehicle could be stabilized. After the booster package
was jettisoned, the missile was stabilized and decelerating in the retrofire mode
by 148 seconds. The sustainer continued thrusting in this attitude until 282.9
seconds when reentry heating apparently caused sustainer shutdown and vehicle
breakup.
464. 5039D AC-59 (FLTSATCOM), 6 Aug 81, Response Mode NA, Flight Phase 1 and 5:
The basic mission was accomplished although three increasingly severe shock
events were recorded at 56.2, 70,7, and 120.8 seconds. The structural damage
sustained by the spacecraft severely limited on-orbit operations.
466. 76E (NAVSTAR VII), 18 Dec 81: Response Mode 2, Flight Phase 1: Shortly after
clearing the launch tower at an altitude of about two tower heights, the thrust
performance of the Bl engine began to decay. The engine was shut down
completely by 7.4 seconds. The unbalanced thrust caused the missile to pitch over
to the right, and travel horizontally for about one second. It then pitched toward
the ground. A small explosion . occurred about one-third of the way down,
followed by a larger explosion when the missile impacted the ground directly
behind the launch pad about 19 seconds after liftoff. Cause of the engine failure
was plugging of the gas-generator fuel-cooling parts that resulted in a gas-
generator bum-through.
477. 5042G AC-62 (Intelsat V), 9 Jun 84, Response Mode 4T, Flight Phase 4:
Performance was normal until an abnormal shock event occurred at
Atlas/Centaur separation. Subsequent data indicated that a Centaur oxygen tank
leak resulted in a loss of 1483 pounds of LOX during Centaur first burn. The leak
resulted in the LOX tank pressure falling below the LH2 tank pressure, which led
to collapse of the intermediate bulkhead during the coast phase.
Bulkhead
collapse caused unexpected tumbling forces during coast. The Centaur engines
restarted after coast, but burned for only 6 or 7 secorids of a planned 90-second
bum.
489. 5048G AC-67 (FLTSATCOM F-6), 26 Mar 87, Response Mode 4T, Flight Phase 1:
Vehicle performance was normal till 48.4 seconds, when the vehicle was struck by
lightning. As a result, the guidance computer commanded a hard right tum
which caused vehicle breakup due to inertial and aerodynamic loads. RSO sent
destruct at 70.7 seconds.
498. 5050 AC-70 (BS-3H COMSAT), 18 Apr 91, Response Mode 4T, Flight Phase 3:
Atlas performance was normal. Although both Centaur main engines began the
start sequence properly, the C-1 turbo-machinery decelerated and stopped,
leaving the C-1 engine thrust at the ignition level. Air entering through the stuck-
open check valve liquefied and froze in the LH2 pump and gear box of the C-1
9/10/96
131
RTI
Community corrections
No user corrections yet.
Comments
No comments on this document yet.
Bottom Reader Ad Slot
Bottom Reader Ad Slot placeholder
If you would like to support SpookStack without paying out of pocket, please consider allowing advertising cookies. It helps cover hosting costs and keeps the archive free to browse. You can change this choice at any time.
Continue Exploring
Explore This Archive Cluster
Broad Topic Hub
Topic Hub
ufo
Related subtopics
Subtopic
Subtopic
Subtopic
Subtopic